4P1L / 4П1Л Siberian Gen4 in Screen mode

Some time ago, I did some initial experiments with the 4P1L (4П1Л) with the screen performing as anode instead. Some DIYers claim the improved sound of the mesh type anodes. Kees Brakenhoff kindly sent me some PL519 to test in screen mode. He has done multiple builds with this mode of operation with great results. Unfortunately I’ve not had the chance yet to build such an amp.

What I could do instead though, was to mod very quickly my 4П1Л preamp to screen mode. It was a very easy and fast modification. I kept the same heating wiring and just adjusted the screen (anode) current down to 10mA: Continue reading “4P1L / 4П1Л Siberian Gen4 in Screen mode”

4P1L (4П1Л) Siberian Gen4 – DHT Preamplifier

The return of the Siberian

After trying out so many DHTs and pre-amplifiers, I decided to wire up my 4P1L preamplifier Gen3 and fit the gyrator board to drive my 4P1L PSE Amplifier.  

I have a pair of 4P1L/4П1Л dated 1968 which are properly burnt in. I’ve used them lately in my previous preamp incarnation with great results. 

The circuit doesn’t need explanation, I think I’ve covered this repeatedly for a long time.  I will only point out the differences:

The main change was fitting a pair of Russian wirewound 27Ω resistors in parallel to get closer to the 15Ω used in this position. I found these Russian wirewound resistors to sound extremely well as filament bias resistors. I tend to be skeptical about the “sound” of some components in circuits, however, they do make a big impact in the cathode of a filament bias arrangement. 

The gyrator has my preferred combination: IXTP08N100D and BSH111BK. I have now an upgraded PCB Rev07 which fits the BSH111BK and similar FET and I will offer them shortly. 

The latter benefits from the 30mA idle current. The result is lower output impedance whilst providing a great frequency response overall.

M3 needs a proper heatsink, it does get hot with about 2W of dissipation. 

How does it perform?

Well, this valve has the reputation of amazing performance and low distortion. The gyrator setup provides the best out of this valve in my view. You can get a flat response as well as great bandwidht from 10Hz up to 3MHz loaded with 100kΩ:

The distortion is very low and is lower than 0.05% below 10Vrms. Dominant H2 with a lovely harmonic profile characteristic of this valve. 

How does it sounds?

i’ve been listening and using this valve extensively since 2011. I have to say that it sounds amazing. I never get tired of its sounds. Before I listened to a 4P1L-4P1L system and found a slight edge on the sound (probably due to its H3 component) which I don’t hear on my system. The drive, clarity and tone is amazing. It can drive the 4P1L PSE perfectly well and you get a strong and clear bass. Very powerful. My +600 hours 4P1L are very quiet in this setup, no microphonic noise. I don’t have even dampers in the 4P1L sockets!

Anyway, if you need 19dB (x9) gain in your system or you need a driver for your  SE amp, then this is the valve to go. I Still can be found cheaply and is a great contender to the thoriated tungsten filament DHTs like 01a and VT-25. 

Build this one and enjoy!

4P1L: pump up the current!

Background

I’m a firm believer than sharing knowledge and experience is the best way forward to continue learning yourself. It always pay pack at some point. This time Paul Prinz, a fellow implementer of the 3B7 DHT Preamp using the gyrator PCB, came back with a great suggestion. He found a MOSFET which could do high drain currents, it has high transconductance and most importantly the parasitic capacitances were low even close to the BF862. Hooray, I thought.  We may have a great solution here to use the gyrator load for currents above 25mA and with similar performance to the great BF862. There are some other depletion MOSFETs that can do high currents, however they all have relatively high capacitances and low transconductances when VDS is low, like in the cascoded gyrator circuit. 

The BSH111BK is an enhancement MOSFET, so doesn’t have a “depletion” behaviour like the jFETs. This isn’t a problem as the bias voltage can be set by the reference CCS. 

For comparison, here is a brief summary of the key characteristics of these three devices:

  BF862 BSH111BK MMBFJ310L 
Ptot  (W) 0.3 0.3 0.225
VDSmax (V) 20 55 25
VGS off (V) -1.2   -4
IDSS (mA) 25 210 60
Gfs (mS) 45 640 18
Ciss (pF) 10 19.1 5
Crss (pF) 1.9 1.5 2.5
Coss (pF)   2.7  

Continue reading “4P1L: pump up the current!”

Abusing the Gyrator Load

On my previous post, I covered my initial build work on the gyrator test mule using the gyrator PCB. I did all the lovely soldering work (which I do enjoy not like milling or drilling) and proceeded to do several tests.

Some interesting observations based on my abuse of the gyrator which yielded on several MOSFETs and JFET damaged as a result:

  • CCS reference: I used an external multi turn 5KΩ potentiometer via lead cables. I wired it incorrectly and that contributed to one of the initial faults. Be sure you look carefully on this if you use an external pot. if you use the on-board trimpot, this is not an issue.
  • JFET: this is the interesting one. If you want to run the lower JFET at very low biasing current for a larger jFET (e.g. J310) you will find that the JFET needs to operate close to cut-off voltage (somewhere between -2 and -6V). This VGS required will definitely forward bias the Zener protection diode D1 and prevent from reaching lower bias current (I found it about 10mA for J310). To resolve this you just need to add a back to back zener as shown below. This isn’t a problem for an BF862 or a 2SK170 as their cut-off voltages are quite small.
  • Failure: if you abuse the FETs, they will die. And if they die you will get a nice short across them and you will measure nearly HT at the mu output. Just replace the MOSFET and JFET (probably both are damaged)

Continue reading “Abusing the Gyrator Load”

Driving the 45 in A2 (part 2)

On the previous post I explored how more power could be extracted from the 45 in class A2. Here is a first draft circuit using the 4P1L as the driver stage with a mu-follower gyrator load to provide current with low output impedance:

45 SE Class A2 dc-coupled

3.5W can be obtained with 13Vpp input signal. Clearly a pre-amp is required, but that is the output level I’m currently getting from my preamp so should be fine. The LND150 CCS reference can be optimised and derived from the stable 280V.

Not a bad idea, just an additional power supply to avoid any nasty cap in the path.